BLR厌氧反应器处理垃圾焚烧厂渗滤液工程运行效能

殷鹏飞, 赵明星, 阮文权. BLR厌氧反应器处理垃圾焚烧厂渗滤液工程运行效能[J]. 环境工程学报, 2015, 9(3): 1155-1160. doi: 10.12030/j.cjee.20150327
引用本文: 殷鹏飞, 赵明星, 阮文权. BLR厌氧反应器处理垃圾焚烧厂渗滤液工程运行效能[J]. 环境工程学报, 2015, 9(3): 1155-1160. doi: 10.12030/j.cjee.20150327
Yin Pengfei, Zhao Mingxing, Ruan Wenquan. Project operation effect of BLR anaerobic reactor for leachate treatment of garbage incineration plant[J]. Chinese Journal of Environmental Engineering, 2015, 9(3): 1155-1160. doi: 10.12030/j.cjee.20150327
Citation: Yin Pengfei, Zhao Mingxing, Ruan Wenquan. Project operation effect of BLR anaerobic reactor for leachate treatment of garbage incineration plant[J]. Chinese Journal of Environmental Engineering, 2015, 9(3): 1155-1160. doi: 10.12030/j.cjee.20150327

BLR厌氧反应器处理垃圾焚烧厂渗滤液工程运行效能

  • 基金项目:

    国家科技支撑计划项目(2011BAC11B05)

  • 中图分类号: X703

Project operation effect of BLR anaerobic reactor for leachate treatment of garbage incineration plant

  • Fund Project:
  • 摘要: 采用1 100 m3 BLR(biogas-lift reactor)厌氧反应器对垃圾焚烧厂渗滤液进行工程化处置,接种污泥为消化污泥,正常运行温度控制在(33±2)℃,启动负荷为1 kg COD/(m3·d),120 d后容积负荷达到10 kg/(m3·d)并稳定运行,出水COD浓度为4 500~6 500 mg/L,COD去除率为88%~92%,出水VFA含量为200~600 mg/L,pH值稳定在7.4~7.7,出水SS含量为1 000 mg/L左右,并可观察到沉降性较好的颗粒化污泥。反应器运行初期将VFA/ALK控制在1.6以内,系统并未因VFA积累而酸化崩溃,运行后期VFA/ALK值小于0.3,系统稳定运行。运行过程中进水氨氮浓度从400 mg/L升高到2 200 mg/L,未发现氨氮对厌氧生物处理的明显抑制现象。垃圾渗滤液中平均每去除1 kg COD产生沼气量为0.32 m3。
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  • [1] Chimenos J. M., Segarra M., Fernández M. A., et al. Characterization of the bottom ash in municipal solid waste incinerator. Journal of Hazardous Materials, 1999, 64(3): 211-222
    [2] Xu Fu, Huang Zhenxing, Miao Hengfeng, et al. Identical full-scale biogas-lift reactors (BLRs) with anaerobic granular sludge and residual activated sludge for brewery wastewater treatment and kinetic modeling. Journal of Environmental Sciences, 2013, 25(10): 2031-2040
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  • 收稿日期:  2014-03-06
  • 刊出日期:  2015-03-05
殷鹏飞, 赵明星, 阮文权. BLR厌氧反应器处理垃圾焚烧厂渗滤液工程运行效能[J]. 环境工程学报, 2015, 9(3): 1155-1160. doi: 10.12030/j.cjee.20150327
引用本文: 殷鹏飞, 赵明星, 阮文权. BLR厌氧反应器处理垃圾焚烧厂渗滤液工程运行效能[J]. 环境工程学报, 2015, 9(3): 1155-1160. doi: 10.12030/j.cjee.20150327
Yin Pengfei, Zhao Mingxing, Ruan Wenquan. Project operation effect of BLR anaerobic reactor for leachate treatment of garbage incineration plant[J]. Chinese Journal of Environmental Engineering, 2015, 9(3): 1155-1160. doi: 10.12030/j.cjee.20150327
Citation: Yin Pengfei, Zhao Mingxing, Ruan Wenquan. Project operation effect of BLR anaerobic reactor for leachate treatment of garbage incineration plant[J]. Chinese Journal of Environmental Engineering, 2015, 9(3): 1155-1160. doi: 10.12030/j.cjee.20150327

BLR厌氧反应器处理垃圾焚烧厂渗滤液工程运行效能

  • 1. 江南大学环境与土木工程学院, 无锡 214122
基金项目:

国家科技支撑计划项目(2011BAC11B05)

摘要: 采用1 100 m3 BLR(biogas-lift reactor)厌氧反应器对垃圾焚烧厂渗滤液进行工程化处置,接种污泥为消化污泥,正常运行温度控制在(33±2)℃,启动负荷为1 kg COD/(m3·d),120 d后容积负荷达到10 kg/(m3·d)并稳定运行,出水COD浓度为4 500~6 500 mg/L,COD去除率为88%~92%,出水VFA含量为200~600 mg/L,pH值稳定在7.4~7.7,出水SS含量为1 000 mg/L左右,并可观察到沉降性较好的颗粒化污泥。反应器运行初期将VFA/ALK控制在1.6以内,系统并未因VFA积累而酸化崩溃,运行后期VFA/ALK值小于0.3,系统稳定运行。运行过程中进水氨氮浓度从400 mg/L升高到2 200 mg/L,未发现氨氮对厌氧生物处理的明显抑制现象。垃圾渗滤液中平均每去除1 kg COD产生沼气量为0.32 m3。

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